6σ Student Case Study UMICHCE - Oil Fill Level

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    Oil Fill Level Project

    Solving Problems with Labor and Maintenance Costs

    Prepared by:

    DR

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    Oil Fill Level Project DR 2

    Executive Summary

    Problem Statement

    Reports of incorrect oil level at assembly plants and dealers have been reported as a significant issue. In response to

    these reports, management implemented two inspection points to protect the customer.

    The focus and business need of this project is to eliminate hard cost associated with packout inspection. This expense is

    $130,000 annually. Secondary benefits include the opportunity to rebalance operation OP400 and reduce internal

    repair costs. And because inspection is not 100% effective, a reduction in DPM will directly improve quality to the

    customer.

    Problem Solving Approach Utilized

    The DMAIC process was utilized throughout this project. A cross-section of both qualitative and quantitative tools was

    used. Some key methods were ishikawa diagrams, run charts, hypothesis testing, and distribution analysis. Pp and Ppk

    values were the primary indicators of performance.

    Major Project Results and Recommendations

    After review of the current state data, the focus of this project was oil level variation. The key contributor was the cold

    test stands. This was highlighted by a change in strategy to focus on oil weight, instead of oil level, as our response

    variable. As you can see in the main body of the report, the other main contributors, such as location of the oil and

    component variation, were eliminated.

    A design flaw within the oil delivery circuit was the primary issue responsible for the variation. The oil circuit had a

    bleed off circuit that provided an internal leak path. This bleed off circuit was the safety mechanism used to relieve

    pressure in the oil delivery system during maintenance activity. In other words, this meant that oil counted as entering

    the engine was being returned to the storage tank. To correct this issue a normally open solenoid valve was installed.

    As a result of this project and the changes mentioned above and in the body of the report, the 100% inspection was

    eliminated at packout and OP400. The packout inspection removal resulted in a $130,000 savings by redeploying two

    team members. The removal of OP400 inspection resulted in a (3) second reduction in work time. And more

    importantly, the housekeeping and safety issues associated with oil on the floor at OP400 are no longer a concern.

    Another potential benefit was realized during this project. It was found that all engines are being filled above nominal

    by approximately 230ml per engine. This amounts to $65,000 per year savings potential.

    Control mechanisms were implemented to maintain the current condition. An audit process was implemented to

    provide ongoing variable data. This data will be used to provide real-time feedback about the oil delivery system health.

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    Oil Fill Level Project DR 3

    1.0 Improvement Opportunity: Define Phase

    1. 1 Discussion of the process being examined and problem addressed

    Reports of incorrect oil level at assembly plants and dealers have been reported as a significant issue. In response to

    these reports, management implemented two inspection points to protect the customer. One inspection point was

    added to the final assembly operation at OP400. A second inspection point was added in packout located after the

    engines are racked for shipment. See the diagram below.

    OP10

    Line Start

    OP400

    Line End

    123

    = Inspection Point

    Packout

    Inspection

    Area

    Cold Test

    (Oil Fill Equipment)

    Shipping

    The measurement method used by assembly plants and dealers is based on a visual inspection of the dipstick after warm

    the engine and allowing five minutes for oil to drain back into the oil pan. Specification limits at the assembly plant are c

    defined as 10-24mm above the bottom of the safe zone. See the diagram below labeled as CSA Audit Range.

    Differences in engine conditions (angle and temperature) and measurement technique exist between the engine plant an

    vehicle assembly plant. At the engine plant, a graduated hand gage is used for measurement. At vehicle assembly a

    production dipstick is used. Mapping was completed to align the measurement values between the two sources. A follo

    hypothesis test yielded a high p-value. This indicated no significant difference exists between the values obtained using

    two measurement methods. In other words, we could now take measurements using the engine plants gage at time of

    predict the assembly plant measurements. See below for details.

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    Oil Fill Level Project DR 5

    Stand1

    Stand2

    Stand3

    Fill pt 1

    Fill pt 2

    Initial Fill

    (~ 3.5 quarts)

    Oil Test & Running

    Torque

    (~ .7 quarts)

    Top Off

    (~ 1.5 quarts)

    1

    2

    3

    Step Fill Pt

    1/2

    2

    1

    Oil

    Supply

    Totalizer

    Orifice

    Engine

    1.2 Key measurements defining project successo Reduction in common cause variation and achievement of 1.44 Ppk.o Removal of packout inspection and the associated expense.o Removal of operation OP400 inspection needs for 1st time-pass engines.

    1.3 Project scope

    The focus and business need of this project is to eliminate hard cost associated with packout inspection. This expense is

    $130,000 annually. Secondary benefits include the opportunity to rebalance OP400 and reduce internal repair costs.

    And because inspection is not 100% effective, a reduction in DPM will directly improve quality to the customer. The

    vehicle assembly plant is referred to as the customer for this project. The DMAIC process was followed.

    Historical records related to out-of-specification claims were not available. The quantity and condition of non-

    conforming engines sent to the customer were unknown. In addition, engines found at the internal inspection points

    were not being recorded. We had little more than subjective opinions about the current status at the beginning of this

    project.

    This project will focus on 1st time pass engines only. Reworked engines are viewed as special cause situations due to the

    human interface and are removed from the data analysis. Additionally, turbo engines have different specifications and

    will not be included in the study. Lessons learned from this project will be applied to these cases.

    2.0 Current State of the Process: Measure Phase

    2.1 Current performance level

    As mentioned above, there was no objective data available to assess the current state. This required initial data is

    gathered to facilitate problem definition. Measurements were taken at three inspection locations; OP400, packout, and

    stable. Data from the stable condition was used as the current state and provided a baseline for the project.

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    Oil Fill Level Project DR 6

    2422201816141210

    LSL USL

    LSL 10

    Target *

    USL 24

    Sample Mean 19.5446

    S ample N 258

    StDev(Within) 1.71902

    StDev(Ov erall) 2.02296

    Process Data

    C p 1.36

    C P L 1. 85

    CPU 0.86

    Cpk 0.86

    P p 1.15

    P P L 1. 57

    PPU 0.73

    Ppk 0.73

    C pm *

    O verall Capability

    Pote ntial (Within) Capability

    P PM < LS L 0.00

    PPM > USL 11627.91

    PPM Tota l 11627.91

    Observed P erformance

    P PM < LS L 0.01

    PPM > USL 4773.10

    PPM Tota l 4773.11

    Exp. Within Performance

    P PM < LS L 1.19

    PPM > USL 13817.46

    PPM Total 13818.65

    Exp. O verall Performance

    Within

    Overall

    Baseline PCA for stable, -rework, -turbo, -cf

    The current state data was stratified to analyze stand-to-stand and model-to-model differences (see below). Hypothesis

    testing confirmed that not one stand or model was significantly different than the others. But from a practical

    standpoint, cold test stand 2 had the highest standard deviation. Focus was placed on this stand for testing and

    improvements. Lessons learned would be shared to the other two cold test stands. In addition, the three locations

    were analyzed to understand the impact of time on the oil level readings. Below are results.

    3

    2

    1

    3.002.752.502.252.001.751.50

    coldteststand

    95% Bonferroni Confidence Intervals for StDevs

    Test Statistic 8.87

    P -V alu e 0. 012

    Test Statistic 3.35

    P -V alu e 0. 037

    Bartlett's Test

    Levene's Test

    Baseline TEV, stable, al l stands, -rework, -turbo, -cf

    CH

    CG

    CE

    CA

    BA

    AA

    3.02.52.01.51.0

    model

    95% Bonferroni Confidence Intervals for StDevs

    Test Statistic 4.03

    P -Valu e 0. 545

    Test Statistic 0.79

    P -Valu e 0. 557

    Bartlett's Test

    Levene's Test

    Baseline Test for Equal Variance for stable by model, -rework, -cf

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    Oil Fill Level Project DR 7

    2422201816141210

    0.20

    0.15

    0.10

    0.05

    0.00

    oil level adj

    Density

    10 24

    16.69 2.262 258

    18.56 2.112 201

    19.54 2.023 258

    Mean StDev N

    OP400.1

    packout

    stable

    location

    measure

    oil level

    Normal

    Baseline Histogram for all locations w/ updated specs, -rework, -turbo, -cf

    Below is a bulleted list that summarizes the project findings before progressing to the analyze phase. The analysis tool

    and conclusion is listed for each. Some of the supporting evidence is shown in the appendix.

    - The Engine Plants hand gage measurement technique is acceptable.o Analysis method paired measurement scatter ploto Conclusion this method can be used to measure oil level throughout the project

    - Difference between the engine plants readings (stable) and assembly plant readings are insignificant. (This istrue because the engine plants gage was adjusted to correlate properly.)

    o Analysis method hypothesis testing f-test, p-value .683 t-test, p-value .418

    o Conclusion The Engine Plant can use the same specification limits as the assembly plant 10-24mm

    - Engine rack angle has an impact on the oil level readings.o Analysis method distribution analysis & square root of sum of squares

    1 = 2mm Estimated s impact of .25mm

    oConclusion oil level measurements will be taken while engine is mounted on pallet prior to beingplaced in engine rack

    - No cold test stand is significantly different than the other two stands. From a practical standpoint stand 2 isworse than the others.

    o Analysis method hypothesis testingo Conclusion testing will be completed on stand 2 and read across to the other stands

    - No model is significantly different than all the others.o Analysis method hypothesis testingo Conclusion any model can be used for analysis

    - Oil level readings change significantly from the time of fill to the time of shipment.

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    Oil Fill Level Project DR 8

    o Analysis method run chart, distribution analysis, hypothesis testing p-value 0.000 (t-test) OP400 (~5 min after fill) = 0 (baseline) Packout (~1 hr after fill) = +2mm Stable (~24 hrs after fill) = +3mm Mean differences are significant, variation differences are not significant

    o Conclusion target oil levels must account for change based on measurement location, the total change level between fill and shipment is approximately 3mm

    2.2 Identification of key variables

    The diagram below was developed to break the potential causes into (4) distinct categories. A fishbone shown in the

    appendix lists individual potential causes along with the rationale for elimination throughout the project.

    Oil Level

    Variation

    @ Dipstick

    Oil Supply

    Location of Oil

    Components

    Measurement

    2.3 Identification of target performance levels or project goals

    Based on the current state data, this project is primarily focused on variation reduction. The project goal is to identify

    the primary sources of variation affecting oil level and therefore eliminate the need for costly inspection. The

    quantifiable targets are shown below.

    o 1.94 Pp (s = 1.2mm)o 1.44 Ppk (accounts for 1.5s mean shift)o < 10 DPM

    3.0 Analysis and Findings: Analyze Phase

    In the measure phase above we realized stand-to-stand and model-to-model differences were insignificant. A look at thi

    in time series highlighted drastic changes in oil level between consecutive engines.

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    Oil Fill Level Project DR 9

    12/5/

    083:35PM

    12/5/

    082:37PM

    12/3/0

    812:46PM

    12/2/0

    812:45AM

    12/2/0

    812:43AM

    12/2/0

    812:26AM

    12/2/0

    812:12AM

    12/2/0

    812:10AM

    12/2/0

    812:04AM

    12/2/0

    812:03AM

    12/2/0

    812:01AM

    12/1/0

    811:56PM

    12/1/0

    811:53PM

    12/1/0

    811:36PM

    12/1/0

    811:15PM

    12/1/0

    811:04PM

    23

    22

    21

    20

    19

    18

    17

    16

    15

    14

    cold test date/time

    oilleveladj

    Baseline Time Series Plot for stable, stand 2, CA, -rework, -cf

    6mm change

    in (20) minute

    time period

    The oil delivery cycle includes an air purge just before the coupler disconnects from the engine. A quick test of this

    system was performed. The results showed this function was insignificant to oil level.

    20

    10

    0

    3.02.52.01.51.00.50.0

    blowdowntime

    95% Bonferroni Confidence Intervals for StDevs

    Test Statistic 0.05

    P -Valu e 0.978

    Test Statistic 0.05

    P -Valu e 0.954

    Bartlett's Test

    Levene's Test

    Blow Down Test for Equal Variances at stable

    In the diagram at the beginning of section 2.2, (4) categories of variance are shown. A strategy change was made at this

    point in the project. The response being measured was changed from oil level to oil weight. This change provided an

    opportunity to split the potential causes. Below illustrates the rationale.

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    Oil Fill Level Project DR 10

    Oil Level

    Variation

    @ Dipstick

    Oil Supply

    Location of Oil

    Components

    Measurement

    Dictionary split can be

    made between these by

    using oil weight.

    Addressed in

    measure phase.

    Consecutive engines were weighed before and after oil addition. Similar to the original baseline data, this test resulted i

    consecutive engines having drastic differences. This focused our attention to the oil supply. In other words, location of o

    components can not influence oil weight within the engine and therefore the variation must be caused by the cold test st

    (oil delivery system).

    As mentioned in section 1.1, oil delivery can be broken down into three segments. In effort to make another strategy sp

    each segment was analyzed individually and the variation reviewed. No segment showed separation. In other words, alsegments contributed relatively equally to the overall variation. This indicated the issue was not segment dependent.

    3a23a2321a

    0.1

    0.0

    -0.1

    -0.2

    -0.3

    segment

    actual-r

    ecorded

    Individual Plot of actual-recorded by segment

    .14 qt

    .08 qt

    .14 qt

    .22 qt .09 qt

    Points indicate the amount

    of error between actual

    volume delivered &

    volume the stand believes

    is present

    Square root of sum of squares = .061 qts

    (accounts for 51% of entire process)

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    Oil Fill Level Project DR 11

    Next we reviewed the oil delivery circuit and its components with the OEM of the cold test stands. Upon inspection of t

    circuit it was realized a bleed off circuit offered a potential internal leak. This meant that oil counted as entering the e

    could be redirected. The bleed off circuit was in place to depressurize the circuit during maintenance and eliminate sa

    concerns. Testing of a blocked bleed off circuit was completed and this had a significant impact as seen in the f-test belo

    using the square root of sum of squares, a 25% (.53mm) reduction in standard deviation was calculated. See below and

    appendix for details.

    123b

    123

    0.40.30.20.10.0

    segment_1

    95% Bonferroni Confidence Intervals for StDevs

    123b

    123

    10.310.210.110.09.99.89.7

    segment_1

    oil wt_1

    Test Statistic 8.27

    P -Valu e 0.004

    Test Statistic 14.27

    P -Valu e 0.002

    F-Test

    Levene's Test

    Test for Equal Variance of bleed off circuit affect

    The totalizer was the last potential cause evaluated. As mentioned above, this is the device that pumps and counts oil

    as it enters the engine. After inspection and testing it was found that this unit had no significant impact but it did have

    some practical impact. In the control phase are the steps we took to address it. See the summary graphs shown in the

    improve phase for the overall impact.

    4.0 Recommendations: Improve Phase

    Based on the analysis above, improvement was made to the cold test stands to address the bleed off circuit. A

    normally open solenoid valve was installed. This valve remains closed during oil delivery to close off the circuit and

    eliminate the internal leak possibility. When the cold test stands are E-stopped prior to maintenance, the solenoid valve

    will open and relieve pressure and the associated safety concern. See below.

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    Oil Fill Level Project DR 12

    OilSupply

    Totalizer

    Bleed Off Loop

    Solenoid

    ValveAdded Valve

    Orifice

    Engine

    In addition, the totalizer for cold test stand 2 was replaced after finding an insufficient seal between the piston ringsand bores.

    A summary of final results for model CG are shown below. It can be seen by the hypothesis testing and distribution

    analysis that all three cold test stands have made the required improvement. Each of them is achieving a standard

    deviation of 1.2mm or less. This standard deviation results in the required Pp. Adjustments can easily be made to

    achieve the required Ppk.

    2322212019181716

    0.6

    0.5

    0.4

    0.3

    0.2

    0.1

    0.0

    oil level adj

    Density

    21 0.8660 11

    18.27 0.8148 31

    Mean StDev N

    0

    6

    sequence

    Normal

    cold test stand = 3

    Histogram of seq 0 vs 6, CG, std 3

    2322212019181716

    0.6

    0.5

    0.4

    0.3

    0.2

    0.1

    0.0

    oil level adj

    Density

    18.92 1.428 12

    20.16 1.069 35

    Mean StDev N

    0

    6

    sequence

    Normal

    cold test stand = 2

    Histogram of seq 0 vs 6, CG, std 2

    2322212019181716

    0.6

    0.5

    0.4

    0.3

    0.2

    0.1

    0.0

    oil level adj

    Density

    18.43 0.9759 7

    19.13 0.6734 43

    Mean StDev N

    0

    6

    sequence

    Normal

    cold test stand = 1

    Histogram of seq 0 vs 6, CG, std 1

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    Oil Fill Level Project DR 13

    Impact of

    Changes

    Baseline

    Original valve install

    Totalizer swap

    Encoder swap

    Valve swap

    The final step was to remove the inspection points at packout and OP400. This was completed on 3/1/10 and control

    mechanisms were implemented. These are discussed in the control phase.

    5.0 Monitoring and Control: Control Phase

    As control mechanisms, the following items were completed. As mentioned in the define phase, this project was

    targeted at 1st time pass engines. As a result you will notice 100% inspection remains on all repair engines. This

    accounts for approximately 1% of the engines.

    - Equipment drawings were updated to reflect the newly installed solenoid valve.- Information about the oil delivery circuit modification was shared with The Engine Plants new product launch

    team.

    - Preventative maintenance activity was added to monitor the condition of the totalizer.- An audit process was implemented requiring the OP400 team member to inspect oil level, on a frequency basis,

    for 1st time pass engines and input values into the HMI. Repair engines remain at 100%. In both cases these

    values are sent to the corporate server and can be accessed at any time to monitor the process.

    - Improved the OP400 oil removal process by adding a coupler that locates on the dipstick boss and removes apredetermined amount of oil. This is used for repair engines.

    - Improved the OP400 oil addition process by adding a graduated beaker with associated millimeter markings.This is used for repair engines.

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    Oil Fill Level Project DR 14

    6.0 Conclusion

    As a result of this project and the changes mentioned above, the 100% inspection was eliminated at packout and OP400.

    The packout inspection removal resulted in a $130,000 savings by redeploying two team members. The removal of

    OP400 inspection resulted in a (3) second reduction in work time. And more importantly, the housekeeping and safety

    issues associated with oil on the floor at OP400 are no longer a concern.

    Another potential benefit was realized during this project. It was found that all engines are being filled above nominal

    by approximately 230ml per engine. This amounts to $65,000 per year savings potential. All model types will be

    adjusted to nominal over the next several months to attain these savings.

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    Oil Fill Level Project DR 15

    Appendices

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    Oil Fill Level Project DR 16

    Oil weight

    variation

    Man Machine

    Material Method

    Oil passages on block

    Oil pan volume

    Incorrect oil type

    Crank oil hole volume

    Rear seal

    -

    -

    -

    Incorrect gage used

    Gage read incorrectly

    A

    A: checked against standard

    B: completed MSA

    C: inspected oil lines

    D: would not cause variation

    E: would not impact oil weight

    F: test completed, no impact

    H: test confirmed bleed off circuit

    impact of .53mm sigma

    I: test completed, some impact

    Rationale

    Incorrect gage design

    Blow down

    Oil drainback

    Correction factor

    Recycle

    Accumulator

    Oil circuit external leak

    Totalizer (oil meter)

    Oil heater

    Valve sequencing logic

    B

    C

    D

    A D

    Oil circuit internal leak

    Parameter settingsA

    E

    E

    E

    E

    H

    F

    Engine angle during checkE

    I

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