6σ Student Case Study UMICHCE - Oil Fill Level
-
Upload
ccaballerog206 -
Category
Documents
-
view
223 -
download
0
Transcript of 6σ Student Case Study UMICHCE - Oil Fill Level
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
1/17
Oil Fill Level Project
Solving Problems with Labor and Maintenance Costs
Prepared by:
DR
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
2/17
Oil Fill Level Project DR 2
Executive Summary
Problem Statement
Reports of incorrect oil level at assembly plants and dealers have been reported as a significant issue. In response to
these reports, management implemented two inspection points to protect the customer.
The focus and business need of this project is to eliminate hard cost associated with packout inspection. This expense is
$130,000 annually. Secondary benefits include the opportunity to rebalance operation OP400 and reduce internal
repair costs. And because inspection is not 100% effective, a reduction in DPM will directly improve quality to the
customer.
Problem Solving Approach Utilized
The DMAIC process was utilized throughout this project. A cross-section of both qualitative and quantitative tools was
used. Some key methods were ishikawa diagrams, run charts, hypothesis testing, and distribution analysis. Pp and Ppk
values were the primary indicators of performance.
Major Project Results and Recommendations
After review of the current state data, the focus of this project was oil level variation. The key contributor was the cold
test stands. This was highlighted by a change in strategy to focus on oil weight, instead of oil level, as our response
variable. As you can see in the main body of the report, the other main contributors, such as location of the oil and
component variation, were eliminated.
A design flaw within the oil delivery circuit was the primary issue responsible for the variation. The oil circuit had a
bleed off circuit that provided an internal leak path. This bleed off circuit was the safety mechanism used to relieve
pressure in the oil delivery system during maintenance activity. In other words, this meant that oil counted as entering
the engine was being returned to the storage tank. To correct this issue a normally open solenoid valve was installed.
As a result of this project and the changes mentioned above and in the body of the report, the 100% inspection was
eliminated at packout and OP400. The packout inspection removal resulted in a $130,000 savings by redeploying two
team members. The removal of OP400 inspection resulted in a (3) second reduction in work time. And more
importantly, the housekeeping and safety issues associated with oil on the floor at OP400 are no longer a concern.
Another potential benefit was realized during this project. It was found that all engines are being filled above nominal
by approximately 230ml per engine. This amounts to $65,000 per year savings potential.
Control mechanisms were implemented to maintain the current condition. An audit process was implemented to
provide ongoing variable data. This data will be used to provide real-time feedback about the oil delivery system health.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
3/17
Oil Fill Level Project DR 3
1.0 Improvement Opportunity: Define Phase
1. 1 Discussion of the process being examined and problem addressed
Reports of incorrect oil level at assembly plants and dealers have been reported as a significant issue. In response to
these reports, management implemented two inspection points to protect the customer. One inspection point was
added to the final assembly operation at OP400. A second inspection point was added in packout located after the
engines are racked for shipment. See the diagram below.
OP10
Line Start
OP400
Line End
123
= Inspection Point
Packout
Inspection
Area
Cold Test
(Oil Fill Equipment)
Shipping
The measurement method used by assembly plants and dealers is based on a visual inspection of the dipstick after warm
the engine and allowing five minutes for oil to drain back into the oil pan. Specification limits at the assembly plant are c
defined as 10-24mm above the bottom of the safe zone. See the diagram below labeled as CSA Audit Range.
Differences in engine conditions (angle and temperature) and measurement technique exist between the engine plant an
vehicle assembly plant. At the engine plant, a graduated hand gage is used for measurement. At vehicle assembly a
production dipstick is used. Mapping was completed to align the measurement values between the two sources. A follo
hypothesis test yielded a high p-value. This indicated no significant difference exists between the values obtained using
two measurement methods. In other words, we could now take measurements using the engine plants gage at time of
predict the assembly plant measurements. See below for details.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
4/17
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
5/17
Oil Fill Level Project DR 5
Stand1
Stand2
Stand3
Fill pt 1
Fill pt 2
Initial Fill
(~ 3.5 quarts)
Oil Test & Running
Torque
(~ .7 quarts)
Top Off
(~ 1.5 quarts)
1
2
3
Step Fill Pt
1/2
2
1
Oil
Supply
Totalizer
Orifice
Engine
1.2 Key measurements defining project successo Reduction in common cause variation and achievement of 1.44 Ppk.o Removal of packout inspection and the associated expense.o Removal of operation OP400 inspection needs for 1st time-pass engines.
1.3 Project scope
The focus and business need of this project is to eliminate hard cost associated with packout inspection. This expense is
$130,000 annually. Secondary benefits include the opportunity to rebalance OP400 and reduce internal repair costs.
And because inspection is not 100% effective, a reduction in DPM will directly improve quality to the customer. The
vehicle assembly plant is referred to as the customer for this project. The DMAIC process was followed.
Historical records related to out-of-specification claims were not available. The quantity and condition of non-
conforming engines sent to the customer were unknown. In addition, engines found at the internal inspection points
were not being recorded. We had little more than subjective opinions about the current status at the beginning of this
project.
This project will focus on 1st time pass engines only. Reworked engines are viewed as special cause situations due to the
human interface and are removed from the data analysis. Additionally, turbo engines have different specifications and
will not be included in the study. Lessons learned from this project will be applied to these cases.
2.0 Current State of the Process: Measure Phase
2.1 Current performance level
As mentioned above, there was no objective data available to assess the current state. This required initial data is
gathered to facilitate problem definition. Measurements were taken at three inspection locations; OP400, packout, and
stable. Data from the stable condition was used as the current state and provided a baseline for the project.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
6/17
Oil Fill Level Project DR 6
2422201816141210
LSL USL
LSL 10
Target *
USL 24
Sample Mean 19.5446
S ample N 258
StDev(Within) 1.71902
StDev(Ov erall) 2.02296
Process Data
C p 1.36
C P L 1. 85
CPU 0.86
Cpk 0.86
P p 1.15
P P L 1. 57
PPU 0.73
Ppk 0.73
C pm *
O verall Capability
Pote ntial (Within) Capability
P PM < LS L 0.00
PPM > USL 11627.91
PPM Tota l 11627.91
Observed P erformance
P PM < LS L 0.01
PPM > USL 4773.10
PPM Tota l 4773.11
Exp. Within Performance
P PM < LS L 1.19
PPM > USL 13817.46
PPM Total 13818.65
Exp. O verall Performance
Within
Overall
Baseline PCA for stable, -rework, -turbo, -cf
The current state data was stratified to analyze stand-to-stand and model-to-model differences (see below). Hypothesis
testing confirmed that not one stand or model was significantly different than the others. But from a practical
standpoint, cold test stand 2 had the highest standard deviation. Focus was placed on this stand for testing and
improvements. Lessons learned would be shared to the other two cold test stands. In addition, the three locations
were analyzed to understand the impact of time on the oil level readings. Below are results.
3
2
1
3.002.752.502.252.001.751.50
coldteststand
95% Bonferroni Confidence Intervals for StDevs
Test Statistic 8.87
P -V alu e 0. 012
Test Statistic 3.35
P -V alu e 0. 037
Bartlett's Test
Levene's Test
Baseline TEV, stable, al l stands, -rework, -turbo, -cf
CH
CG
CE
CA
BA
AA
3.02.52.01.51.0
model
95% Bonferroni Confidence Intervals for StDevs
Test Statistic 4.03
P -Valu e 0. 545
Test Statistic 0.79
P -Valu e 0. 557
Bartlett's Test
Levene's Test
Baseline Test for Equal Variance for stable by model, -rework, -cf
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
7/17
Oil Fill Level Project DR 7
2422201816141210
0.20
0.15
0.10
0.05
0.00
oil level adj
Density
10 24
16.69 2.262 258
18.56 2.112 201
19.54 2.023 258
Mean StDev N
OP400.1
packout
stable
location
measure
oil level
Normal
Baseline Histogram for all locations w/ updated specs, -rework, -turbo, -cf
Below is a bulleted list that summarizes the project findings before progressing to the analyze phase. The analysis tool
and conclusion is listed for each. Some of the supporting evidence is shown in the appendix.
- The Engine Plants hand gage measurement technique is acceptable.o Analysis method paired measurement scatter ploto Conclusion this method can be used to measure oil level throughout the project
- Difference between the engine plants readings (stable) and assembly plant readings are insignificant. (This istrue because the engine plants gage was adjusted to correlate properly.)
o Analysis method hypothesis testing f-test, p-value .683 t-test, p-value .418
o Conclusion The Engine Plant can use the same specification limits as the assembly plant 10-24mm
- Engine rack angle has an impact on the oil level readings.o Analysis method distribution analysis & square root of sum of squares
1 = 2mm Estimated s impact of .25mm
oConclusion oil level measurements will be taken while engine is mounted on pallet prior to beingplaced in engine rack
- No cold test stand is significantly different than the other two stands. From a practical standpoint stand 2 isworse than the others.
o Analysis method hypothesis testingo Conclusion testing will be completed on stand 2 and read across to the other stands
- No model is significantly different than all the others.o Analysis method hypothesis testingo Conclusion any model can be used for analysis
- Oil level readings change significantly from the time of fill to the time of shipment.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
8/17
Oil Fill Level Project DR 8
o Analysis method run chart, distribution analysis, hypothesis testing p-value 0.000 (t-test) OP400 (~5 min after fill) = 0 (baseline) Packout (~1 hr after fill) = +2mm Stable (~24 hrs after fill) = +3mm Mean differences are significant, variation differences are not significant
o Conclusion target oil levels must account for change based on measurement location, the total change level between fill and shipment is approximately 3mm
2.2 Identification of key variables
The diagram below was developed to break the potential causes into (4) distinct categories. A fishbone shown in the
appendix lists individual potential causes along with the rationale for elimination throughout the project.
Oil Level
Variation
@ Dipstick
Oil Supply
Location of Oil
Components
Measurement
2.3 Identification of target performance levels or project goals
Based on the current state data, this project is primarily focused on variation reduction. The project goal is to identify
the primary sources of variation affecting oil level and therefore eliminate the need for costly inspection. The
quantifiable targets are shown below.
o 1.94 Pp (s = 1.2mm)o 1.44 Ppk (accounts for 1.5s mean shift)o < 10 DPM
3.0 Analysis and Findings: Analyze Phase
In the measure phase above we realized stand-to-stand and model-to-model differences were insignificant. A look at thi
in time series highlighted drastic changes in oil level between consecutive engines.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
9/17
Oil Fill Level Project DR 9
12/5/
083:35PM
12/5/
082:37PM
12/3/0
812:46PM
12/2/0
812:45AM
12/2/0
812:43AM
12/2/0
812:26AM
12/2/0
812:12AM
12/2/0
812:10AM
12/2/0
812:04AM
12/2/0
812:03AM
12/2/0
812:01AM
12/1/0
811:56PM
12/1/0
811:53PM
12/1/0
811:36PM
12/1/0
811:15PM
12/1/0
811:04PM
23
22
21
20
19
18
17
16
15
14
cold test date/time
oilleveladj
Baseline Time Series Plot for stable, stand 2, CA, -rework, -cf
6mm change
in (20) minute
time period
The oil delivery cycle includes an air purge just before the coupler disconnects from the engine. A quick test of this
system was performed. The results showed this function was insignificant to oil level.
20
10
0
3.02.52.01.51.00.50.0
blowdowntime
95% Bonferroni Confidence Intervals for StDevs
Test Statistic 0.05
P -Valu e 0.978
Test Statistic 0.05
P -Valu e 0.954
Bartlett's Test
Levene's Test
Blow Down Test for Equal Variances at stable
In the diagram at the beginning of section 2.2, (4) categories of variance are shown. A strategy change was made at this
point in the project. The response being measured was changed from oil level to oil weight. This change provided an
opportunity to split the potential causes. Below illustrates the rationale.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
10/17
Oil Fill Level Project DR 10
Oil Level
Variation
@ Dipstick
Oil Supply
Location of Oil
Components
Measurement
Dictionary split can be
made between these by
using oil weight.
Addressed in
measure phase.
Consecutive engines were weighed before and after oil addition. Similar to the original baseline data, this test resulted i
consecutive engines having drastic differences. This focused our attention to the oil supply. In other words, location of o
components can not influence oil weight within the engine and therefore the variation must be caused by the cold test st
(oil delivery system).
As mentioned in section 1.1, oil delivery can be broken down into three segments. In effort to make another strategy sp
each segment was analyzed individually and the variation reviewed. No segment showed separation. In other words, alsegments contributed relatively equally to the overall variation. This indicated the issue was not segment dependent.
3a23a2321a
0.1
0.0
-0.1
-0.2
-0.3
segment
actual-r
ecorded
Individual Plot of actual-recorded by segment
.14 qt
.08 qt
.14 qt
.22 qt .09 qt
Points indicate the amount
of error between actual
volume delivered &
volume the stand believes
is present
Square root of sum of squares = .061 qts
(accounts for 51% of entire process)
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
11/17
Oil Fill Level Project DR 11
Next we reviewed the oil delivery circuit and its components with the OEM of the cold test stands. Upon inspection of t
circuit it was realized a bleed off circuit offered a potential internal leak. This meant that oil counted as entering the e
could be redirected. The bleed off circuit was in place to depressurize the circuit during maintenance and eliminate sa
concerns. Testing of a blocked bleed off circuit was completed and this had a significant impact as seen in the f-test belo
using the square root of sum of squares, a 25% (.53mm) reduction in standard deviation was calculated. See below and
appendix for details.
123b
123
0.40.30.20.10.0
segment_1
95% Bonferroni Confidence Intervals for StDevs
123b
123
10.310.210.110.09.99.89.7
segment_1
oil wt_1
Test Statistic 8.27
P -Valu e 0.004
Test Statistic 14.27
P -Valu e 0.002
F-Test
Levene's Test
Test for Equal Variance of bleed off circuit affect
The totalizer was the last potential cause evaluated. As mentioned above, this is the device that pumps and counts oil
as it enters the engine. After inspection and testing it was found that this unit had no significant impact but it did have
some practical impact. In the control phase are the steps we took to address it. See the summary graphs shown in the
improve phase for the overall impact.
4.0 Recommendations: Improve Phase
Based on the analysis above, improvement was made to the cold test stands to address the bleed off circuit. A
normally open solenoid valve was installed. This valve remains closed during oil delivery to close off the circuit and
eliminate the internal leak possibility. When the cold test stands are E-stopped prior to maintenance, the solenoid valve
will open and relieve pressure and the associated safety concern. See below.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
12/17
Oil Fill Level Project DR 12
OilSupply
Totalizer
Bleed Off Loop
Solenoid
ValveAdded Valve
Orifice
Engine
In addition, the totalizer for cold test stand 2 was replaced after finding an insufficient seal between the piston ringsand bores.
A summary of final results for model CG are shown below. It can be seen by the hypothesis testing and distribution
analysis that all three cold test stands have made the required improvement. Each of them is achieving a standard
deviation of 1.2mm or less. This standard deviation results in the required Pp. Adjustments can easily be made to
achieve the required Ppk.
2322212019181716
0.6
0.5
0.4
0.3
0.2
0.1
0.0
oil level adj
Density
21 0.8660 11
18.27 0.8148 31
Mean StDev N
0
6
sequence
Normal
cold test stand = 3
Histogram of seq 0 vs 6, CG, std 3
2322212019181716
0.6
0.5
0.4
0.3
0.2
0.1
0.0
oil level adj
Density
18.92 1.428 12
20.16 1.069 35
Mean StDev N
0
6
sequence
Normal
cold test stand = 2
Histogram of seq 0 vs 6, CG, std 2
2322212019181716
0.6
0.5
0.4
0.3
0.2
0.1
0.0
oil level adj
Density
18.43 0.9759 7
19.13 0.6734 43
Mean StDev N
0
6
sequence
Normal
cold test stand = 1
Histogram of seq 0 vs 6, CG, std 1
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
13/17
Oil Fill Level Project DR 13
Impact of
Changes
Baseline
Original valve install
Totalizer swap
Encoder swap
Valve swap
The final step was to remove the inspection points at packout and OP400. This was completed on 3/1/10 and control
mechanisms were implemented. These are discussed in the control phase.
5.0 Monitoring and Control: Control Phase
As control mechanisms, the following items were completed. As mentioned in the define phase, this project was
targeted at 1st time pass engines. As a result you will notice 100% inspection remains on all repair engines. This
accounts for approximately 1% of the engines.
- Equipment drawings were updated to reflect the newly installed solenoid valve.- Information about the oil delivery circuit modification was shared with The Engine Plants new product launch
team.
- Preventative maintenance activity was added to monitor the condition of the totalizer.- An audit process was implemented requiring the OP400 team member to inspect oil level, on a frequency basis,
for 1st time pass engines and input values into the HMI. Repair engines remain at 100%. In both cases these
values are sent to the corporate server and can be accessed at any time to monitor the process.
- Improved the OP400 oil removal process by adding a coupler that locates on the dipstick boss and removes apredetermined amount of oil. This is used for repair engines.
- Improved the OP400 oil addition process by adding a graduated beaker with associated millimeter markings.This is used for repair engines.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
14/17
Oil Fill Level Project DR 14
6.0 Conclusion
As a result of this project and the changes mentioned above, the 100% inspection was eliminated at packout and OP400.
The packout inspection removal resulted in a $130,000 savings by redeploying two team members. The removal of
OP400 inspection resulted in a (3) second reduction in work time. And more importantly, the housekeeping and safety
issues associated with oil on the floor at OP400 are no longer a concern.
Another potential benefit was realized during this project. It was found that all engines are being filled above nominal
by approximately 230ml per engine. This amounts to $65,000 per year savings potential. All model types will be
adjusted to nominal over the next several months to attain these savings.
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
15/17
Oil Fill Level Project DR 15
Appendices
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
16/17
Oil Fill Level Project DR 16
Oil weight
variation
Man Machine
Material Method
Oil passages on block
Oil pan volume
Incorrect oil type
Crank oil hole volume
Rear seal
-
-
-
Incorrect gage used
Gage read incorrectly
A
A: checked against standard
B: completed MSA
C: inspected oil lines
D: would not cause variation
E: would not impact oil weight
F: test completed, no impact
H: test confirmed bleed off circuit
impact of .53mm sigma
I: test completed, some impact
Rationale
Incorrect gage design
Blow down
Oil drainback
Correction factor
Recycle
Accumulator
Oil circuit external leak
Totalizer (oil meter)
Oil heater
Valve sequencing logic
B
C
D
A D
Oil circuit internal leak
Parameter settingsA
E
E
E
E
H
F
Engine angle during checkE
I
-
7/31/2019 6 Student Case Study UMICHCE - Oil Fill Level
17/17